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CarComplaints.com Notes: Here's a disturbing trend for the 2002 Nissan Altima: the engine starts burning oil like crazy, the catalytic converter goes bad, the head gasket blows and eventually the entire engine needs replacement. Sound familiar? Like a script from a horror film, these Altimas seem doomed to fail around 95k miles.
8.3
pretty bad- Typical Repair Cost:
- $1,950
- Average Mileage:
- 142,600 miles
- Total Complaints:
- 7 complaints
Most Common Solutions:
- replace engine, catalytic converter and exhaust system (4 reports)
- not sure (1 reports)
- replace engine (1 reports)
- replace engine/catalytic converter/exhaust system (1 reports)
engine problem
Helpful websites
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A D V E R T I S E M E N T S
BELOW IS MY VEHICLE HISTORY SINCE 2006 - IF ANYONE CAN OFFER ADVICE IT WOULD BE GREATLY APPRECIATED. THIS CAR SEEMS TO HAVE THE CHECK ENGINE LIGHT COME OUT AT LEAST 2-3 TIMES A YEAR SINCE +80,000 MILES. I HAVE SPENT THOUSANDS OF DOLLARS AND HAVE ONLY BEEN PLAGUED WITH THE SAME ERRORS; MISFIRES, CRANK/CAM SENSORS ,INTAKE MANIFOLDS ETC.
7/7/06 - (41,619 miles) Concern: Check engine light is on and vehicle is overheating. - cause: bad radiator - correction : replaced radiator and t-stat - total : 299.20
2/25/08 - (64,744 miles) reprogram ECM & IAVL as per recall R0712 (Selma Nissan)
11/13/08 - (73,350 miles) Concern: Check engine light is on. - Cause: Found code for at solenoid overheating malfunction - Correction: based on the testing we found that the solenoid is operating per the tech book but the transmission fluid is very bad. need to complete a transmission fluid exchange. Tech performed BG transmission fluid exchange to remove old burned fluid. -total : 278.97
7/16/09 - (80,442 miles) Concern: Vehicle overheating. Service engine light is on. - cause: Found coolant leaking into #3 cylinder due to the head gasket becoming bad. - correction: replaced engine head gasket, car had code P0302 cylinder 2 misfire checked and found that head gasket was blown. Replaced lower and upper radiator hoses. Replaced t-stat. - total: 1,570.37
12/9/09 - (87,625 miles) Concern: Heater not working. - cause: Found cooling system is low on refrigerant. Pressurized system and found leak from rear hose. Car leaking coolant from hose under electric throttle actuator . Found that there was a small hose under intake that was leaking coolant. - correction: replaced hose that was leaking. - total: 172.54
9/27/10 (92,405 miles) Concern: check engine light on. - cause: cylinder #2 misfire - correction : Replaced spark plugs - total: 210.00
10/27/12 (112,264 miles) concern: brake concern and dragging/grinding when turning left - cause: unknown - correction: Replaced power steering fluid. Replaced spark plugs. Replaced SERP belt. - total: 415.78
6/28/13 (117,526 miles) Concern: car would not start - correction: replaced battery - total: 103.30
6/28/13 (117,526 miles) Concern: problems starting vehicle, when vehicle would start gas pedal did not respond - cause: Code P1612 Immobilizer System Malfunction. Found defective alternator. - correction: replace alternator - total: 524.56
8/22/14 (131,647 miles) concern: check engine light on, battery light on, seat belt light on, brake light on - cause: Code P0335 - crankshaft position sensor A circuit malfunction. Found crankshaft sensor signal out of range intermittent. - correction: Replace crankshaft position sensor. - total: $278
5/16/15 (146,493 miles) concern: Vehicle stopped running multiple times while driving (engine died). Rough idle. Engine light on. - cause: Tech found code P0304 cylinder 4 misfire. Power valve screws and plate came loose. Screws were found in cylinder 4 chamber and were smashing spark plug tip. - correction: Replaced lower intake manifold. -total: 547.03
5/23/15 (146,524 miles) concern: rough left turn - cause: tie rod -correction: Replace tie rod. Transmission fluid service. Service alignment. - total: 420.91
8/25/15 (154,197 miles) concern: Vehicle stopped running multiple times while driving (engine died). - cause: unknown - technician did not find any error codes but recommended replacement of cam sensor and crank sensor - estimated total to replace: $603.15 (declined service at that time)
- mo_1980, San Francisco, CA, US